Wild Rose ~ Quarry Hunslet

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dewintondave
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Post by dewintondave » Mon Feb 08, 2016 1:45 am

Whilst waiting for some paint to dry... I've been cutting out the frames from sheet steel. I have a lifetime supply of 1.6 mm :)

It's hard work with a hacksaw. Filing the edges flat was aided with a long straight edge and sighting through.
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Here's the frame blanks cut to length
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Last edited by dewintondave on Sun Nov 24, 2019 3:31 am, edited 2 times in total.
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Dave

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Post by dewintondave » Sun Feb 28, 2016 9:02 am

I've been cutting those lovely cut-outs in the frames, lots of sawing and filling. Then lots of drilling for spacers, and heaps of 8 BA tapping in the spacers. I start the tap square in the bench drill. But, first I remove the quill return spring...



Filing, filing
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Frames and spacers
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Last edited by dewintondave on Sun Nov 24, 2019 3:31 am, edited 2 times in total.
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Dave

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Post by dewintondave » Mon Mar 07, 2016 6:32 am

I've been working on the buffer beams.  The chassis is bolted together.  It was nice to do some turning again, the axle bearings were turned yesterday from gunmetal.

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I couldn't resist sliding the wheels on

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I've a supply of 8BA screws from my local supplier.
Last edited by dewintondave on Sun Nov 24, 2019 3:30 am, edited 2 times in total.
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Dave

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Post by dewintondave » Fri Mar 11, 2016 9:47 am

The buffer beam height is perfect for the LGB stock...

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Last edited by dewintondave on Sun Nov 24, 2019 3:29 am, edited 2 times in total.
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Dave

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Post by dewintondave » Sat Mar 26, 2016 5:03 am

At last a rolling chassis. The coupling rods are finished. I shaped the cranks in blocks of two blanks soldered together, the profile is a bit different between the pairs, so I'll put each pair on their own side of the loco, and not mix them.

Checking the clearances
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Rolling chassis
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This is how I modify screws. I needed 1/4" AF for the cranks, to keep the rods on, but had no bar stock. I converted four 4 BA screws into 8 BA
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Now I need to think about the cylinders...
Last edited by dewintondave on Sun Nov 24, 2019 3:22 am, edited 1 time in total.
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Dave

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Post by Dannypenguin » Sat Mar 26, 2016 9:43 am

Wow this is all looking really good, I'm following this with great interest :thumbright:
Dan

Visit the PFLR website - http://poultonfarmlightrailway.webs.com/
Dean Forest Railway Society website - http://dfrsociety.org/

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Post by dewintondave » Sun May 08, 2016 4:19 am

A month ago I made a gentle start on the smokebox as I wait for some cylinder materials. I'm using steel sheet for smokebox endplates and wrapper

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Here's the progress so far. I like using roundhead screws for the rivet look, these were used on the live diesel bodywork

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Last edited by dewintondave on Sun Nov 24, 2019 3:24 am, edited 1 time in total.
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Dave

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Post by dewintondave » Sun May 22, 2016 5:39 am

Last weekend I started on a flange to mount the boiler barrel to the smokebox.

Disc blank cut out and mounted on mandrel
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Outside diameter turned
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Centre removed and bored to just pass the boiler barrel OD. Strip cut out and filed flat.
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Strip bent to shape around a handy former. Ready for silver brazing
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Fully brazed. It took many heatings and adjustments to get the strip placed just right. My first go with cadmium free silver solder
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Although a little heat distorted, I was pleased with the concentricity


One week later, boiler barrel fitted to smokebox. 8 BA all the way
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Last edited by dewintondave on Sun Nov 24, 2019 3:28 am, edited 1 time in total.
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Dave

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Post by LNR » Sun May 22, 2016 7:21 am

Hi Dave!
Nice job, be interested to know what you thought of the Cadmium free silver solder, assuming you have used the cadmium stuff before. Hear many reports of it not flowing as well as the old stuff.
I'm afraid I have enough of the cadmium stuff to see me out, so can't see myself changing, but be interested to hear your opinion.
Grant.

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Post by dewintondave » Sun May 22, 2016 9:03 am

Hi Grant, the cadmium free went fine. My old silver solder will soon run out, so I bought a stick of the cadmium free to try. The ring had two spots where it had pooled, I think at the end of the flux line, and me over enthusiastic stick feeding. When the job was finished, I re-fluxed and re-melted them and it flowed nicely without any other aid
Last edited by dewintondave on Sun Nov 24, 2019 3:29 am, edited 1 time in total.
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Dave

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Post by LNR » Sun May 22, 2016 10:46 am

Thanks Dave, I reckon your a game man soldering a ring that thin and then machining it to fit. Concentricity doesn't have to be far out when you involve the lathe. Congratulations.
Grant.

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Post by dewintondave » Sun Jun 12, 2016 10:05 am

I made the chimney base from steel. One of the first operations was to mill the smokebox profile on its base. I did this in the lathe, with my old Emco Unimat 3 flycutter.



After milling, the blank was turned in the lathe, working both handles to get the large radius.
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The job is secured to the mandrel by Loctite 609 retainer
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Lots of heat is required to remove the job from the mandrel, the chimney base is now a lovely blue/black colour
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Last edited by dewintondave on Sun Nov 24, 2019 3:45 am, edited 1 time in total.
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Dave

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Post by Keith S » Sun Jun 12, 2016 3:15 pm

It certainly is a pleasure to see the work in progress. It looks like a fine job so far. I am particularly impressed with the boiler/smokebox flange.

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Post by dewintondave » Mon Jun 13, 2016 10:13 am

Keith S:118494 wrote:It certainly is a pleasure to see the work in progress. It looks like a fine job so far. I am particularly impressed with the boiler/smokebox flange.
Thank you Keith!

---

Moving to the other side of the smokebox, the smokebox door. This is made from a slice of free cutting steel soft soldered to a mandrel after the rear face was turned.

Rear face details just visible
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Profiling the front face
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Finished door still on mandrel
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Hinge straps cut out of 0.6mm sheet with tin snips
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Finished hinges. I used LBSC's "words and music" for the straps and lugs. I had to borrow the roundhead screws from the live diesel
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The door is swinging!
Last edited by dewintondave on Sun Nov 24, 2019 3:49 am, edited 1 time in total.
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Dave

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Post by philipy » Mon Jun 13, 2016 12:52 pm

Dave,
The big problem with your work is that I ran out of superlatives long ago! As always, I'm in awe.
Philip

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Post by dewintondave » Tue Jun 14, 2016 10:00 am

philipy:118509 wrote:Dave,
The big problem with your work is that I ran out of superlatives long ago! As always, I'm in awe.
Thank you!
Last edited by dewintondave on Sun Nov 24, 2019 3:50 am, edited 1 time in total.
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Dave

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Post by dewintondave » Sun Jul 03, 2016 5:53 am

It was time to start on the chimney. I started at the top.

Gunmetal was used for the chimney cap. The blank was Loctited to the mandrel
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Marking out the upper curved part
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I filed this curved surface
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Rough turned
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Finish turned
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Finished part
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Tall chimney version
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Cross-bar fitted
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Out on the line!
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It was a lovely morning for a cigar and coffee!
Last edited by dewintondave on Sun Nov 24, 2019 5:51 am, edited 1 time in total.
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Dave

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Post by robyholmes » Tue Jul 05, 2016 9:37 pm

Fantastic! Love seeing your work.

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Post by dewintondave » Mon Jul 25, 2016 9:50 am

robyholmes:118836 wrote:Fantastic! Love seeing your work.
Thank you!

---

I made a start on the cylinders. I like to use commercial plain bronze bearings for oscillator cylinders. They have a very good surface finish.

The port faces were bored in the lathe using the exact same set-up as was used for my large de Winton. Bored for the cylinders to be able to be soft soldered to them.

The faceplate required counter balance weights

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The port face is soft soldered to the faceplate angle plate

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I want the rear covers to be removable. I like screwcutting so decided to thread the end covers and the cylinder. An internal tool was ground for the cylinder, this took days... I've used 40 tpi as the pitch. As the threads were short I turned the chuck by hand. My wrist was aching like a teenager's afterwards!

Image

Image
Last edited by dewintondave on Sun Nov 24, 2019 5:53 am, edited 1 time in total.
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Dave

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Post by dewintondave » Sat Oct 22, 2016 8:37 am

I thought I'd tackle the boiler next so that I could see where everything will go. I've been very slowly progressing.

A supply of 1.5 mm copper sheet, 2", and 1/2" copper pipe was already on hand. I've recently received some more sticks of the cadmium free silver solder (brazing rods) from Macc Models, I'm ready to make a sizeable investment in the boiler - lots of silver.

Some 4 mm thick steel was bought to make flanging formers. I was able to reuse a boiler endplate flanging former from my first loco build; the small De Wintons. Flanging is very satisfying with frequent stops for annealing the copper sheet.

Rounding off the throatplate / backhead former
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Rework #1: Removing a thin strip from the wrapper using the piercing saw. The throatplate is already brazed in place.
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Backhead and former
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Firebox former with unformed plate
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Progress so far
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Last edited by dewintondave on Sun Nov 24, 2019 5:55 am, edited 1 time in total.
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Dave

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