Updates will be sporadic, depending on how long it takes to do anything interesting enough to write about..
This Ruston & Hornsby 40DL was our first operational loco on-site in 1979, but parked up since the '90s with gearbox issues.
Restoring it for our 50th anniversary in 2022 was a short-notice decision, and our mechanical engineer Ryan got it going, right there in the siding. The little loco limped into the workshop under it's own power.

Ryan put a mammoth effort into the loco, making one good gearbox out of two bad ones, fixed a lot of body rust and machined numerous parts.
But for the lack of volunteers to complete it, the Ruston spent our 50th missing it's wheels, bonnet and cab, covered in mess.
We have far too many half-finished projects and overdue restorations scattered to the wind.
It's taking up space in the workshop and holding up projects we actually need, such as: A third open carriage, the large enclosed RM carriage, (along with two others longer term) '29 Fowler 0-6-0DM, the Baguley 0-6-0DM, new firefighting wagon (prerequisite for a return to steam) and 4+ different steam loco restorations. All of which are stalled projects. And much, much more besides..
Now, the Ruston has only a handbrake by design, so we can't use it on passenger trains. This means it's only good for shunting or trackwork - something we have Gemco and Netherdale for. And, we'll have to evict something from the loco shed to house it.
It is at least small enough to put on a tilt tray and take to model railway or machinery shows. Or loan to other railways.
So then, I want this show pony out of the workshop. Being a limited-use loco, "good enough" work is the order of the day.
My usual perfectionism is out the window on this one.

19/10/2024
Ryan had started building the frame of a new cab in 2022, so I finished that, including a few parts salvaged from the old corroded cab.
Hitting a roadblock for need of more steel and welding gas, I turned to getting the loco permanently back on it's wheels.
The axleboxes were soaked in solvent for a week, before a thorough cleaning and repaint. The bearings were badly worn, but good enough to reuse once Ryan had re-machined them.

10/11/24
Axleboxes rebuilt, springs refurbished and wheels painted, the loco could then be lowered back onto it's wheels.

25/01/2025
Attention then turned to the unusual (and very leaky) radiator. Many weeks of welding, swearing, tapping, filling, painting and bodging saw the lower tank/bonnet front & radiator cores refitted to the chassis.

01/02/25
Gemco on a short navvy working. This loco has always been a stalwart of ANGRMS, and received an extensive overhaul in (I think?) early 2022.

With the radiator assembled (not quite as leak-free as thought) Ruston 279,567 of 1949 was started for the first time since it came into the workshop. We have yet to put it in gear, or even refit the chain drive to the wheels. But it's a milestone and the best day I've had in the workshop in years.
Speaking of years, it's been ten to the day, since I joined ANGRMS.

16/02/25
Another trip down to Woodford in my Model A Ford, saw work continue on the radiator and bonnet. All being well, I should have the radiator finished and the bonnet refitted next weekend.
























