Cracker GTi
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- Trainee Driver
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- Joined: Wed Nov 14, 2007 2:34 pm
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- Trainee Driver
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- Joined: Wed Nov 14, 2007 2:34 pm
today was an exciting day, as I got the chassis silver soldered together. Plonked it on the hearth and heated it up, solder penetration is reasonable enough. The amount of tarnish on it afterwards was such that I chucked it in the sandblaster and gave it a good going over, looked lovely when it came out, and had a good key for the paint. I put some grey primer on to keep it from rusting.
Other jobs included drilling the steam ports in the frames, and modifying the reverser valve. This was done by plating over the usual outlets for the Mamod loco and drilling holes through the back to bring the steam round 90 degrees instead.
the axle steel arrived today, and I shall be making these just as soon as the wheels are sorted out.
Other jobs included drilling the steam ports in the frames, and modifying the reverser valve. This was done by plating over the usual outlets for the Mamod loco and drilling holes through the back to bring the steam round 90 degrees instead.
the axle steel arrived today, and I shall be making these just as soon as the wheels are sorted out.
proudly flying in the face of convention
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today was a fun one. Got the loco up on its wheels and rolling. Reamed out the bearings, and using a collet lathe (to ensure accuracy) made bushes for the wheels to make them gauge adjustable. I then made some brass keeps for the ends of the axles to keep them in place. By the end of the day the chassis was rolling along nicely and all the gears meshing up. Next job is the crankshaft!
proudly flying in the face of convention
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- Hancockshire
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- Location: Stranraer
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the boiler should be fine, its been proportionally enlarged along with the rest of the chassis from the original Cracker drawings which as we all know works fine.Hancockshire:53967 wrote:Boiler looks a little small. I suppose that's the price to pay if you model the wrong gauge
I could fit a larger boiler if I wanted to but this one will be satisfactory. A twin cylinder variant would certainly require one. Gauge is optional ;)
don't start the gauge thing, its boring.
proudly flying in the face of convention
- tom_tom_go
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oh dear life really got in the way of progress on poor little Cracker
not to worry though! Today I went down the railway workshops and set myself the challenge of getting the crankshaft finished, and replace the duff axle on one wheelset. Once the axle was made two flywheels were made up, one recessed and one with a crankpin fitted. The actual crankshaft was made and fitted, I trimmed it to length once the flywheels were on. The tiny weeny gear had a boss made and was put on with a setscrew.
Having made sure it turned over (it was a bit stiff) I smothered everything in oil, fired up the air compressor and deep joy, it ran. I ran it at 50 psi for about 30 mins in both directions, and it loosened up nicely. When I was done I sprayed some 3 in 1 heavy foam degreaser on it and left it for 10 mins, washing it down afterwards. Can't have it covered in oil!
So there we are, a bit more progress :D
not to worry though! Today I went down the railway workshops and set myself the challenge of getting the crankshaft finished, and replace the duff axle on one wheelset. Once the axle was made two flywheels were made up, one recessed and one with a crankpin fitted. The actual crankshaft was made and fitted, I trimmed it to length once the flywheels were on. The tiny weeny gear had a boss made and was put on with a setscrew.
Having made sure it turned over (it was a bit stiff) I smothered everything in oil, fired up the air compressor and deep joy, it ran. I ran it at 50 psi for about 30 mins in both directions, and it loosened up nicely. When I was done I sprayed some 3 in 1 heavy foam degreaser on it and left it for 10 mins, washing it down afterwards. Can't have it covered in oil!
So there we are, a bit more progress :D
proudly flying in the face of convention
- Sir Clothem Cap
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